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"Dedicated to assisting companies to operate Safer by reducing human error"
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HUMAN
PERFORMANCE IN MAINTENANCE
CASE STUDY #1 "Death
of an Airline" DC-8-61
“We must learn from
the mistakes of others
because we
will never live long enough to make them
all ourselves” For more information regarding this case study contactGordon
Dupont System
Safety Services Website:
www.system-safety.com Email:
dupontg@system-safety.com Phone/Fax:
604 526-3993
This
case study and the video is available from the Maintenance And Ramp Safety
Society (MARSS) 5750
Cedarbridge Way Richmond,
BC Canada V6X 2A7 Contact
Website:
www.marss.org Email
marss@marss.org Telephone:
604 207-9100 This case study may be reproduced for use with the training video SYNOPSIS The aircraft
took off from Runway 34L at Jeddah, Saudi Arabia with 247 passengers and 14 crew
members on board. During the take-off roll,
the front tires, then the front wheels failed on the main undercarriage and
remnants of the failed tires were burning when the landing gear was retracted
after take-off. A fire developed within the
main gear wheel wells causing loss of pressurization, loss of hydraulics,
structural damage and finally loss of control. During the final stages of
the approach to runway 34C, witnesses reported a significant increase of fire and smoke
and the aircraft dived and rolled to crash 2,875 meters short of the runway
threshold. History of Deployment July 3:
The aircraft arrived at Jeddah with a group of personnel consisting of 3
complete flight and cabin crews, three mechanics and a project manager for a
21-day deployment to carry out a
series of charter flights for pilgrims from Jeddah to various African countries.
July 4, 5 and 6: The
aircraft made three trips to Conakry, Guinea.
It was then flown to Accra, Ghana where it was grounded for 36 hours for
a repair to the radar system. During
this down time, while waiting for parts, the 125 hour "A" check was
begun (32.5 hours before it was due) and the recorded tire pressures indicated
two(#1 & #4) were low. July 8: The
aircraft flew to Jeddah to pick up a load of pilgrims. July 9:
The aircraft flew one of two
loads of pilgrims to Accra. July 10: The
aircraft landed at Accra with the second load at 0450.
A planned four hour maintenance stop is commenced which called for
changing 5 tires. But the aircraft
was called back to Jeddah by the project manager, the tires were loaded into the
aircraft at 0730 local time and it was flown to Jeddah arriving at 1400 local
time. Routine post-flight
maintenance was carried out and the maintenance crew retired to the hotel at
about 1700. The entire crew, except
for the captain, went shopping and returned at about 2300. July 11:
The crew was awakened at 0300 and arrived at the airport at 0500. The lead mechanic, who would be going with the aircraft in
the cockpit jump seat, carried out a pre-flight check and at 0755, 20 minutes
before departure, with passengers on the aircraft, requested nitrogen for a low
tire. The request was made to a
support facility who informed them that the nitrogen bottles were empty.
Thus he would
have to go to Saudi Airlines to arrange the loan of their equipment.
The project manager was heard to say
"forget it."
The lead mechanic and project manager boarded the aircraft and the flight
engineer signed the pre-flight check as having been completed on the maintenance
release. The Final 30 Minutes The engines were started and
the aircraft was pushed back at 0810. The
outside temperature was 29C as they began to taxi to the runway six
90 degree turns and 17,061 ft. away.
Eleven minutes later they were lined up for take-off on Runway 34L.
The first officer was given control as they began their take-off run at
0827. Within 15 sec, at a speed of
50 kts, an oscillating sound was heard. The
flight engineer said, "What’s that?"
The first officer replied, "We gotta flat tire, you figure?"
The captain responded, "You're not leaning on the brakes,
eh?" The first officer
answered, “No I'm not, I got my feet on the bottom of the rudder." The captain said, "OK."
The captain called, "V1" and two seconds later the first
officer observed, "Sort of a shimmy like if you're riding on one of
those ah thingamajigs." At 51 sec the Captain called,
"Rotate" and nine seconds later reported, "Positive
rate." The FO called for "Gear
up" and the aircraft climbed away. Two minutes and 16 seconds
from brake release, climbing through 1,600 ft. the flight engineer reported, "You've
got four low pressure lights" (said twice). The captain's only response
was, "Yeah." 12 seconds later the flight engineer stated, "losing
pressurization." The first officer requested, "Flaps ten"
twice. The captain called the tower
to inform them that, "we're having a slight pressurization
problem." The tower
mistook them for a Saudi Boeing 737 which was returning with a
pressurization problem. The
first officer then informed the captain, "I got a spoiler light."
"Gear unsafe light." "OK, I thought I blew a tire."
"Flap up." (Second time) "We're losing hydraulics
here" "Flaps"
(third time) The captain then
responded, "The airbrake thing just
broke." The captain was
doing all the radio transmissions and was not using the aircraft call sign.
As more problems cropped up, the flight director came into the cockpit
and reported "...smoke in the back ... real bad."
The captain acknowledged: "Yeah, we're going back, we've got
blown tires...and we got a hydraulic problem Faye, yeah just tell them we'll be
returning to ah Jeddah." Meanwhile
the controller twice reissued their departure clearance. The first officer reported, "I've got no
ailerons," and the captain
responded, "OK, hang on, I've got it." The
controller once more called the aircraft and the captain responded. When given
his departure clearance once more he responded, "OK sir I cannot climb,
I cannot climb. We are at two
thousand feet now declaring an emergency, we have flight control problems."
The controller
finally realized that the DC8 and not the B737 was in an emergency situation
and gave a heading to intercept the final approach.
At about 11 miles from the airport the first of a number of casualties
fell from the aircraft at an altitude of 2,200 feet.
During the final approach, with pieces of aircraft and bodies falling
from it, the weakened empennage failed, the aircraft pitched nose down and from
an altitude of 400 ft. dived at a 70 degree angle into the desert at a speed in
excess of 240 kts. The
disintegrating fuselage pitched over the nose and fragmented in the ensuing
fireball. The wreckage trail spread
1,300 feet long and 650 feet wide with some debris carried over 3,600 feet from
the initial impact. There were no
survivors. The Company The
company began operations about eight years prior to the accident and rapidly
expanded, mostly in the charter operations.
The maintenance on the company aircraft was carried out by a separate
company that was owned by the same person.
Their Company Organization Chart:
Excerpts
from Position Descriptions The
General Manager is responsible to the Chairman of the Board for the
development of a Department capable of efficient and economic accomplishment of all Maintenance
Functions and to provide airworthy, reliable and clean aircraft in a timely
fashion to (airline name) and other Customers at a minimum cost. The
Director of Production is directly responsible to the General Manager for
the efficient Maintenance, Repair and On-Schedule performance....
Organize, direct and control (company name) Maintenance Operations in the
production of on-schedule, safe, clean, aircraft.... The
Director of Engineering and Quality Assurance is responsible to the
General Manager for the efficient and economical performance of the
Quality Department and for the quality of all Maintenance performed on... The
Deployment Maintenance Team The
Maintenance team for the deployment was selected by the lead mechanic and
consisted of himself, an avionics specialist and an A&P mechanic.
While all three were experienced on aircraft, none were holders of a Aircraft Maintenance Engineers’s (AME) license. The
flight engineers on the aircraft were holders of
AME licenses, endorsed on type and
were responsible for certifying the aircraft as airworthy.
The flight engineers did not oversee or do any of the maintenance.
The
Lead Mechanic The 38 year old lead mechanic had been trained in
France and had worked for a number of years in West Africa. While he had worked on DC8s in the past and was considered a
capable mechanic, his knowledge of the DC8 was considered very limited.
His knowledge of English was also very limited and his French was
considered very Parisian. The
company arranged his emigration in order for him to work for them as a senior
mechanic two years previous but he quit after 14 days.
He was rehired as a foreman in training five months before the accident.
This training was on the job training and he received no formal training
from the company. As a condition of
employment he was to obtain his AME license within six months of being hired.
He
was chosen for the Jeddah deployment because of his past experience in West
Africa. Those who worked under him
indicated he was disorganized, unfamiliar with the DC8 and the company’s
maintenance procedures. He indicated to the mechanics on the deployment that he
did not want maintenance operations to cause any flight delays.
It
is said that he had a steady girlfriend and indicated a strong desire to settle
down and move up in the company. He
was responsible directly to the Director of Production but tended to report to
the General Manager. He made daily
calls to the company and never reported any problems.
The aircraft and operation were perfect.
Persons who knew him indicated that he was quite intelligent but
sometimes came across as arrogant He
was responsible for the coordination, accomplishment and recording of all work
done but the certification was done by the flight engineer. The
Project Manager The
41 year old project manager, like the lead mechanic, was a new employee with an
extensive background in passenger services.
His duties were to ensure the smooth flow of passengers for the flights.
He reported to Planning Department. The
Operations Officer The
operations officer was also a spare pilot who looked after the operational
decisions (flight crew scheduling etc) . He
reported to the Operations Department. The
Captain The
47 year old captain spent 28 years in the military; 21 of them as a pilot.
He had joined the company two years earlier as a first officer on the DC8
and after one year he became captain on the DC8.
He had 10,700 hours flying time, 1,000 of which were on the DC8. He
was noted as having a strong personality and went by the book.
It was said that he often lacked confidence in others ability and did not
delegate duties well.
Some crew preferred not to fly with him as he had a tendency to nit-pick
and argue about procedures. During
the 11 minute final flight he took back control of the aircraft as soon as the
first officer indicated he had lost aileron control. He also made 10 radio calls and received 14.
He often made no response or reaction to information given to him. The
First officer The
36 year old first officer had about 8,000 flying hours, 550 of which were in the
DC8. He had obtained his early
flying in the bush and had flown 1,200 hours as a first officer in the Airbus
310 prior to joining the company about one year previous.
He
was noted as being a well liked, out going person with a forceful personality.
He was knowledgeable about the aircraft and confident but did not take
criticism well. It was reported
that he did not like flying with the captain and had decided to just let him do
his thing. The
Flight Engineer The
46 year old flight engineer held a flight engineer’s license as well as an
Aircraft Maintenance
Engineer’s license. He had
served in the military for 24 years, the last 14 as a flight engineer.
He had worked for the company for about two years. He
was described as a quiet,
easy-going person with a conscientious and level-headed approach to his work.
He was very knowledgeable about the aircraft systems and was considered a
professional by his peers. Maintenance
Records During
the deployment, three checklists were used a)
Transit Check: A four page check list to
be used whenever a turn-around was less than four hours. It called to inspect the tires for condition but not
specifically for tire pressure. b)
Preflight Check: An 11 page checklist which was to be done on the first flight
of each day and whenever a stop was more then four hours.
It called for a check of the tire pressures and gave the required
pressure with no tolerance. There was no space to record the pressures and one spot to
initial that they all had been checked. c)
A-Check:
A 20 page checklist which was to be done every 125 hours of flight time.
This check called for the recording of each tire’s pressure in a block
and a sign off for each. The
records showed that this was done at Accra on July 6, 32.5 hours before it was
due. At the time of the accident
8.2 hours remained before the A-check was due and only the 20th page
certification remained to be done. The
company did not have a provision for a progressive A-check. A
forensic inspection of the A-check sheet revealed that #2 tire pressure had been
recorded as 160psi. (180 psi was the called-for pressure)
and #4 was recorded as 155. Both
of these had been altered and recorded as 180 and signed for by the A&P
mechanic. The other tire pressures
were signed for by the avionics specialist. Maintenance
records sent back to the company did not have the flight specifics, such as the
aircraft registration and hours completed in the header portion. The
maintenance records were often filled out at the end of the day and checklists
were done from memory and signed for later. Not
all maintenance defects and maintenance actions were recorded in the aircraft
journey log. Not
all of the maintenance records for the deployment could be located at the
maintenance control center after the accident. The
flight engineers routinely accepted the aircraft for the next flight without
confirming that the checks had been completed.
They would assume the checks were properly completed. There
was some confusion as to what was the correct procedure for recording a tire
with low pressure. It was not clear whether the mechanic should:
1. Record the low pressure
and then top it up.
2. Not record the low
pressure, only the corrected pressure.
3. Record the low pressure
then cross it out and record the corrected
pressure. The
checksheets gave no hint as to which was the correct procedure. The
lead mechanic reported the condition of the aircraft to the company by telephone
every day. Tire
Pressure The
company checklists called for a main tire pressure of 180 psi with no tolerance.
They further stated that if the main tire pressure was below 146 psi., it was to
be changed. If the tire was flat and had been taxied flat then the axle
mate tire must also be changed. Douglas
DC8 Maintenance Manual tire inflation chart gives a graph for the tire pressures
which increase as the aircraft’s gross weight goes up. The chart gives a
tolerance of +5 -0 psi.. At the
aircraft’s gross weight of 325,000 lbs. the tire pressure should be 195 psi.
+5 -0. At the aircraft’s recorded
gross weight the minimum tire pressure should have been 183 psi.
The graph allowed the operator to operate the aircraft at the max gross
weight tire pressure at lower gross weights.
At 180 psi the maximum gross weight would have been 310,000 lbs.
The recorded calculated take off weight was recorded as 313,493 lbs.. The
following is the recommended guidelines for tire replacement.
If less then 15 psi low = add air and record.
(166 psi+)
If more then 15 psi. but less then 30 psi low = change the tire
(151 psi to 165 psi)
If more then 30 psi = change both tires on the axle. (150 psi-) Some
Aircraft Tire Facts The
following material was obtain from a publication put out by Goodyear entitled
“Aircraft Tires Care and Maintenance” No
other tire has to work as hard as an aircraft tire which must support both a
heavy weight and travel at high speed. An
average sized aircraft tire is made up of 50% rubber, 45% fabric and 5% steel by
weight. A
aircraft tire can lose up to 5% of its inflated pressure per day. Heat
build up is one of an aircraft tire’s worst enemies. Most
heat is generated by a traction wave which cycles at the back of a rotating tire
as it regains its shape. Under
inflation is more dangerous as it transfers its load to the other tire, which
deflects more, generating more heat. Nylon
melts at slightly over 200 C (400 F) and at 200 C has lost 50% of its tensile
strength. At
just 10% underinflation a tire has lost 90% of its performance. |